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一体式厌氧氨氧化工艺处理高氨氮污泥消化液的启动
引用本文:杨延栋,黄京,韩晓宇,张亮,张树军,彭永臻.一体式厌氧氨氧化工艺处理高氨氮污泥消化液的启动[J].中国环境科学,2015,35(4):1082-1087.
作者姓名:杨延栋  黄京  韩晓宇  张亮  张树军  彭永臻
作者单位:哈尔滨工业大学市政环境工程学院;中国科学院大学资源与环境学院;北京城市排水集团有限责任公司科技研发中心;北京工业大学,北京市水质科学与水环境恢复工程重点实验室
基金项目:哈尔滨工业大学城市水资源与水环境国家重点实验室项目(QAK201502);国家自然科学基金(21177005)
摘    要:利用新型固定生物膜一活性污泥反应器处理实际污泥消化液,通过接种短程硝化污泥和厌氧氨氧化生物膜填料,逐渐提高进水氨氮浓度并控制溶解氧浓度在0.11~0.42mg/L,系统在65d内实现了短程硝化-厌氧氨氧化反应的启动.反应器系统稳定运行阶段具有良好的污染物去除效果,进水COD和氨氮浓度为921和1120.8mg/L,COD、氨氮和总氮去除率分别为66.8%,99.0%和94.4%,总氮去除负荷为0.27kg N/(m3·d).试验表明采取逐步提高进水中消化液比例的策略,有利于一体式厌氧氨氧化工艺的快速启动.进一步分析发现系统同时存在厌氧氨氧化和反硝化的脱氮途径,对总氮去除的贡献率分别为67.4%~91.1%和8.9%~32.6%.

关 键 词:污泥消化液  自养脱氮  一体化反应器  厌氧氨氧化工艺  

Start-up of one-stage partial nitrification/anammox process treating ammonium-rich reject water
YANG Yan-dong;HUANG Jing;HAN Xiao-yu;ZHANG Liang;ZHANG Shu-jun;PENG Yong-zhen.Start-up of one-stage partial nitrification/anammox process treating ammonium-rich reject water[J].China Environmental Science,2015,35(4):1082-1087.
Authors:YANG Yan-dong;HUANG Jing;HAN Xiao-yu;ZHANG Liang;ZHANG Shu-jun;PENG Yong-zhen
Institution:YANG Yan-dong;HUANG Jing;HAN Xiao-yu;ZHANG Liang;ZHANG Shu-jun;PENG Yong-zhen;School of Municipal and Environmental Engineering,Harbin Institute of Technology;College of Resources and Environment, University of Chinese Academy of Sciences;Research and Development Center of Beijing Drainage Group Technology;Beijing Key Laboratory of Water Science and Water Environmental Restoration, Beijing University of Technology;
Abstract:Partial nitrification/anammox (PN/A) process has become one of the most innovative developments in reject water treatment in recent years. In this study, a one-stage integrated fixed-film activated sludge reactor was used to treat reject water. By inoculating partial nitrification floc sludge and anammox biofilm, gradually increasing ammonium concentration of influent and controlling DO at 0.11~0.42mg/L, the reactor was started successfully in 65days. In the stable phage, the system had a good contaminant removal performance. With influent concentration of COD and ammonium were 921mg/L and 1120.8mg/L respectively, 66.8% COD, 99.0% ammonia and 94.4% total nitrogen were removed respectively and total nitrogen removal rate reached 0.27kgN/(m3·d). The experiment showed that the start-up of PN/A process was promoted by increasing the ratio of reject water in influent gradually. Further analysis revealed that both anammox and denitrification process were present in system. The contributions to total nitrogen removal of anammox and denitrification were 67.4%~91.1% and 8.9%~32.6%, respectively.
Keywords:reject water  autotrophic nitrogen removal  one-stage reactor  anammox  
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