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1.
化学沉淀法处理高浓度氨氮废水的试验研究   总被引:1,自引:0,他引:1  
实验采用磷酸氨镁沉淀法(MAP法)去除垃圾渗滤液中的高浓度氨氮。通过对MgCl2+Na2HPO4^-、MgSO4+Na2HPO4、MgO+Na2HPO4、MgCl2+NaH2PO4、MgSO4+NaH2PO4和MgO+NaH2PO4等六种组合药剂去除氨氮效果的分析比较,得出MgCl2+Na2HPO4对氨氮的去除效果最好。继而对该组合药剂去除氨氮的影响因素进行了优化。结果表明:pH为9.0,反应时1.3为50min,n(Mg^2+):n(NH4^+):n(PO4^3-)为1.2:1:0.9时,氨氮可由原来的2100mg/L降低到317mg/L,去除率达84.9%.  相似文献   

2.
The Murcia Este Wastewater Treatment Plant is the largest wastewater treatment plant in Murcia (Spain). The plant operators have continuously found pipe blockage and accumulation of solids on equipment surfaces during the anaerobic digestion and post-digestion processes. This work studies the precipitation problems in the Murcia Este Wastewater Treatment Plant in order to locate the sources of precipitation and its causes from an exhaustive mass balance analysis. The DAF thickener and anaerobic digester mass balances suggest that most of the polyphosphate is released during excess sludge thickening. Despite the high concentrations achieved in the thickened sludge, precipitation does not occur at this point due to the low pH. The increases in ammonium and pH during anaerobic digestion cause precipitation to take place mainly inside the digesters and in downstream processes. This study shows that 50.7% of the available phosphate is fixed in the digester of which 52.0% precipitates as ammonium struvite, 39.2% precipitates as hydroxyapatite and the remaining 8.8% is adsorbed on the surface of the solids. Thermodynamic calculations confirm the precipitation of struvite and hydroxyapatite and also confirm that potassium struvite does not precipitate in the anaerobic digesters.  相似文献   

3.
Intensive manure application is an important source of diffuse phosphorus (P) pollution. Phosphorus availability from animal manure is influenced by its chemical speciation. The major objective of this study was to investigate the P speciation in raw and anaerobically digested dairy manure with an emphasis on the calcium (Ca) and magnesium (Mg) phosphate phases. Influent and effluent from an on-farm digester in Wisconsin were sampled and sieved, and the 25 to 53 microm size fraction was dried for X-ray powder diffraction (XRD) and P K-edge X-ray absorption near edge structure (XANES) analyses. Struvite (MgNH4PO4.6H2O) was identified in both the raw (influent) and anaerobically digested (effluent) manure using XRD. Qualitative analysis of P K-edge XANES spectra indicated that the Ca orthophosphate phases, except dicalcium phosphate anhydrous (DCPA) or monetite (CaHPO4), were not abundant in dairy manure. Linear combination fitting (LCF) of the P standard compounds showed that 57.0 and 43.0% of P was associated with DCPA and struvite, respectively, in the raw manure. In the anaerobically digested sample, 78.2% of P was present as struvite and 21.8% of P was associated with hydroxylapatite (HAp). The P speciation shifted toward Mg orthophosphates and least soluble Ca orthophosphates following anaerobic digestion. Similarity between the aqueous orthophosphate (aq-PO4), newberyite (MgHPO4.3H2O), and struvite spectra can cause inaccurate P speciation determination when dairy manure is analyzed solely using P K-edge XANES spectroscopy; however, XANES can be used in conjunction with XRD to quantify the distribution of inorganic P species in animal manure.  相似文献   

4.
本文以实际猪场沼气废水为研究对象,以ASBR为反应器,接种厌氧消化污泥培养厌氧氨氧化细菌,厌氧氨氧化阶段成功启动后,研究了厌氧氨氧化脱氮最佳运行工艺。试验研究表明,厌氧氨氧化反应适宜的温度在35(±1)℃之间,适宜的pH在7.5—8.0之间,HRT选用24h。当达到最佳运行参数时,NH4+-N的去除率达到87.6%,NO2- -N的去除率达到99.96%。  相似文献   

5.
To gain more insight into the interactions between anaerobic bacteria and reactor performances (chemical oxygen demand-COD, 2,4 dichlorophenol-2,4 DCP removals, volatile fatty acid-VFA, and methane gas productions) and how they depended on operational conditions the microbial variations in the anaerobic granular sludge from an upflow anaerobic sludge blanket (UASB) reactor treating 2,4 DCP was studied. The study was composed of two parts. In the first part, the numbers of methanogens and acedogens in the anaerobic granular sludge were counted at different COD removal efficiencies. The relationships between the numbers of methanogens, the methane gas production and VFA production were investigated. The COD removal efficiencies increased to 74% from 30% while the number of total acedogens decreased to 10 from 30 cfu ml(-1). The number of total methanogens and acedogens varied between 11 x 10(3) and 10 x 10(9)MPN g(-1) and 10 and 30 cfu ml(-1) as the 2,4 DCP removal efficiencies were obtained between 60% and 99%, respectively. It was seen that, as the number of total acedogens decreased, the COD removal efficiencies increased. However, the number of total methanogens increased as the COD removal efficiencies increased. Correlations between the bacterial number and with the removal efficiencies obtained in different operational conditions were investigated. From the results presented in this paper a high correlation between the number of bacteria, COD removals, methane gas percentage, 2,4 DCP removals and VFA was observed. In the second part, methanogen bacteria in the anaerobic granular sludge were identified. Microbial observations and biochemical tests were applied to identify the anaerobic microorganisms from the anaerobic granular sludge. In the reactor treating 2,4 DCP, Methanobacterium bryantii, Methanobacterium formicicum, Methanobrevibacter smithii, Methanococcus voltae, Methanosarcina mazei, Methanosarcina acetivorans, Methanogenium bourgense and Methanospirillum hungatei were identified.  相似文献   

6.
The literature has paid scarce attention to the modeling of the denitrification-anaerobic digestion process in packed bed biofilm tubular reactors used to treat wastewater. The present study obtained a steady-state model for industrial salmon fishery wastewater treatment in a biofilm tubular reactor, including pH as a variable and the effect of biomass on hydrolysis. The axial profile of the reactor components and process efficiency were predicted with deviations below 6%. The optimal operating zone for the process was found at hydraulic retention time (HRT)>1.5d and inlet protein concentration (S(prot,0))<3000 mgTOCL(-1). Based on our results, we concluded that the removal of organic matter and nitrogen compounds depended mainly on HRT. The effluent pH was mainly affected by the C/N ratio, where a decrease increases pH. Organic matter removal was related with the anaerobic digestion process, while denitrification influenced mostly nitrate and nitrite removal.  相似文献   

7.
In the present work, degradation of rhodamine B, a typical dye effluent commonly observed in chemical processing wastewaters has been investigated using a sonochemical reactor with capacity of 7 L. The reactor consists of an ultrasonic bath equipped with a single large transducer having longitudinal vibrations with operating frequency of 25 kHz and rated power output of 1 kW. The effect of operational conditions such as the rhodamine B initial concentration, operating pH and use of additives such as H(2)O(2), CCl(4) and TiO(2) has been investigated initially. A mathematical model has also been fitted to estimate the rate constant for rhodamine B removal under different operating conditions. Intensification studies have been carried by combining sonochemical oxidation with photocatalytic oxidation under optimized conditions. In all the investigated systems, complete removal of rhodamine B (10 ppm initial concentration) was obtained using a combination of sonochemical reactor and CCl(4). Sonocatalysis (in the presence of TiO(2)) of rhodamine B showed 92% degradation, while sonophotocatalysis gave degradation of 93%. TOC analysis at various optimum conditions was also performed to quantify the extent of mineralization and it was observed that the extent of mineralization is always lower than the extent of removal of parent compound.  相似文献   

8.
Piggery wastes must be treated before their disposal. The high solids content and high chemical oxygen demand of piggery wastes indicated that anaerobic biological treatment could be successfully applied as primary treatment. For that reason, a comparison between upflow anaerobic sludge bed reactor (UASB) and anaerobic fixed bed reactor (AFBR) at a similar organic volumetric loading rate of 5 kg DQO/m3 day was carried out. 60% of the piggery waste COD was removed with the AFBR compared to 40% with the UASB, thus showing a better performance of the AFBR. After 1-h sedimentation secondary process, both anaerobic effluents were treated by ionic exchange with natural zeolite due to their high values of ammoniacal nitrogen (NH+4 plus free NH3). The high removal of nutrients reported (90%) shows zeolite to be a good choice as tertiary treatment.  相似文献   

9.
In the present study, decolorization of a simulated dye waste containing three different triphenylmethane (TPM) dyes--Magenta, Malachite Green and Crystal Violet, was investigated in a laboratory scale, two-stage anaerobic high-rate reactor. The effect of various parameters (influent dye concentration, hydraulic and co-substrate loading rates) on color and COD removal efficiency of the reactor has been studied. It has been shown that the influent dye concentration had little effect on overall COD and color removal efficiency. More than 99% color removal and 96% COD removal efficiency were maintained even at a dye concentration of 500 mg/l and a dye loading rate of 1000 mg/l day. However, a minimum level of glucose as supplementary carbon source is required to maintain the maximum color removal efficiency and it drops appreciably when no glucose is added to the influent. The study also showed that the acidogenic phase of the reaction plays an important role in decolorization of the TPM dyes. In addition, the two-stage anaerobic reactor was observed to have distinct advantages over the single-stage system, as the drop in color and COD removal efficiency of stage 1 are adequately compensated by stage 2 of the reactor especially under high dye loading rates accompanied by low co-substrate loading and under reduced HRTs.  相似文献   

10.
沸石吸附剂脱除炼油废水中低浓度氨氮试验研究   总被引:3,自引:0,他引:3  
沸石(FYH)吸附剂是抚顺石油化工研究院环保所研制开发的一种交换容量大、可再生的吸附剂,用于处理炼油废水中的氨氮时,去除率可以达到90%以上。吸附剂的穿透时间与空速有着直接关系,空速越大,穿透时间越短。吸附剂的交换容量也与空速有关。本试验中,在空速1.2h-1的条件下,吸附剂达到最大交换容量。将氯化钠和氢氧化钠以一定配比配制的再生液可以对FYH吸附剂进行快速而有效的再生。汽提含铵再生液效果很好,脱铵后的再生液中氨氮的浓度为未检出,回收的氨水浓度0.47%~0.68%。经过小试证明该工艺是可行的。  相似文献   

11.
Microbial mineralization of urea and uric acid in poultry litter results in the production of ammonia, which can lead to decreased poultry performance, malodorous emissions, and loss of poultry litter value as a fertilizer. Despite the fact that this is a microbial process, little is known about how the microbial populations, especially ammonia-producing (ureolytic) organisms in poultry litter, respond to litter amendments such as aluminum sulfate (Al(2)(SO(4))(3).14H(2)O; alum). The goal of this study was to measure the temporal changes in total bacterial and fungal populations and urease-producing microorganisms in nontreated litter or litter treated with 10% alum. Quantitative real-time polymerase chain reaction was used to target the bacterial 16S rRNA gene, the fungal 18S rRNA gene, or the urease gene of bacterial and fungal ammonia producers in a poultry litter incubation study. Nontreated poultry litter had relatively high total (2.8 +/- 0.8 x 10(10) cells g(-1) litter) and ureolytic (2.8 +/- 1.3 x 10(8) cells g(-1) litter) bacterial populations. Alum treatment reduced the total bacterial population by 50% and bacterial urease producers by 90% within 4 wk. In contrast, at 16 wk after alum treatment, the fungal population was three orders of magnitude higher in alum-treated litter than in nontreated litter (3.5 +/- 0.8 x 10(7) cells g(-1) litter and 5.5 +/- 2.5 x 10(4) cells g(-1) litter, respectively). The decrease in pH produced by alum treatment is believed to inhibit bacterial populations and favor growth of fungi that may be responsible for the mineralization of organic nitrogen in alum-treated litters.  相似文献   

12.
The presence of ammonia nitrogen in landfill leachates poses a significant problem for treatment plant operators. The nitrification-denitrification process mostly carries out the nitrogen conversion in biological treatment systems. However, recent research shows that other processes by anaerobic ammonia-oxidizing bacteria (Anammox) and ammonia-oxidizing archaea (AOA) were also responsible for the removal of nitrogen in biological systems. In this study, the nitrogen-converting microorganisms in the Bursa Hamitler Leachate Treatment Plant were identified and monitored by using molecular tools. Fluorescent in situ hybridization (FISH) and slot-blot hybridization results showed that the Nitrosomonas and Nitrospira species were the dominant ammonia-oxidizing bacteria (AOB) and nitrite-oxidizing bacteria (NOB), respectively. Quantitative real-time PCR results indicated that AOB, NOB, AOA and Anammox bacteria exist in the leachate treatment plant. However, the removal of ammonia can be ascribed mainly to nitrification because AOB (1.5%) and NOB (11.3%) were predominant among all nitrogen-converting bacteria. The results of the phylogenetic analysis based on amoA and 16S rDNA gene revealed that the uncultured bacterium clone 4-24, Kuenenia stuttgartiensis genome fragment KUST_E and the uncultured Crenarchaeota clone NJYPZT-C1 belong to AOB, Anammox and AOA populations, respectively, and were the dominant species in their cluster.  相似文献   

13.
The relative contribution of reduced nitrogen to acid and eutrophic deposition in Europe has increased recently as a result of European policies which have been successful in reducing SO(2) and NO(x) emissions but have had smaller impacts on ammonia (NH(3)) emissions. In this paper the Fine Resolution Atmospheric Multi-pollutant Exchange (FRAME) model was used to calculate the spatial patterns of annual average ammonia and ammonium (NH(4)(+)) air concentrations and reduced nitrogen (NH(x)) dry and wet deposition with a 5 km × 5 km grid for years 2002-2005. The modelled air concentrations of NH(3) and dry deposition of NH(x) show similar spatial patterns for all years considered. The largest year to year changes were found for wet deposition, which vary considerably with precipitation amount. The FRAME modelled air concentrations and wet deposition are in reasonable agreement with available measurements (Pearson's correlation coefficients above 0.6 for years 2002-2005), and with spatial patterns of concentrations and deposition of NH(x) reported with the EMEP results, but show larger spatial gradients. The error statistics show that the FRAME model results are in better agreement with measurements if compared with EMEP estimates. The differences in deposition budgets calculated with FRAME and EMEP do not exceed 17% for wet and 6% for dry deposition, with FRAME estimates higher than for EMEP wet deposition for modelled period and lower or equal for dry deposition. The FRAME estimates of wet deposition budget are lower than the measurement-based values reported by the Chief Inspectorate of Environmental Protection of Poland, with the differences by approximately 3%. Up to 93% of dry and 53% of wet deposition of NH(x) in Poland originates from national sources. Over the western part of Poland and mountainous areas in the south, transboundary transport can contribute over 80% of total (dry + wet) NH(x) deposition. The spatial pattern of the relative contribution of national sources to total deposition of NH(x) may change significantly due to the general circulation of air.  相似文献   

14.
采用多级内循环厌氧反应器MIC/上升式厌氧反应器UASB串联工艺处理柠檬酸生产排放的高浓度有机废水,其中厌氧处理段的COD去除率>94%,整体COD去除率可达98.3%左右.最终排放口出水COD平均值为190 mg/L,pH值为6~9,达到柠檬酸行业废水排放标准.  相似文献   

15.
Domestic wastewater contains a considerable amount of pathogenic organisms besides non-biodegradable organics. The conventional technologies followed for the treatment of domestic wastewater are less efficient in removing pathogenic organisms despite substantial removal of dissolved organics. The focal theme of the present investigation was to use a chemo-autotrophic activated carbon oxidation (CAACO) system, an immobilized cell reactor using chemoautotrophs (Bacillus sp.) for the treatment of domestic wastewater. The oxidation of organics and Escherichia coli in wastewater is controlled by the parameters space time, O(2)/COD, bed height and cod loading. The scheme comprised of anaerobic treatment, sand filtration and CAACO treatment removed BOD. COD, Total organic carbon (TOC), dissolved protein, total Kjeldhal nitrogen (TKN) and bacterial count (most probable number (MPN)) by 81%, 92%, 84%, 94%, 93% and 99.9997%, respectively. The low concentration of E. coli in the CAACO-treated wastewater was completely eliminated through UV irradiation in 3 min at 254 nm.  相似文献   

16.
Nutrient removal from domestic strength synthetic wastewater by an alternating pumped flow sequencing batch biofilm reactor (APFSBBR) was investigated in this laboratory study. The APFSBBR comprised two reactor tanks (Reactors 1 and 2) with two identical biofilm modules of vertical tubular plastic media with a high specific surface area, one in each tank. The APFSBBR was operated in cycles of four phases: fill, anaerobic, aerobic, and draw. During the fill phase, Reactor 1 was half-filled with domestic strength synthetic wastewater. During the subsequent anaerobic phase, most of the phosphorus release took place from the submerged biofilm in this reactor. In the aerobic phase, the wastewater was circulated by pumps between Reactors 1 and 2, resulting in denitrification at the start of the aerobic phase due to low oxygen concentrations, followed by nitrification and luxury uptake of phosphorus when oxygen concentrations increased. During the draw phase, Reactor 2 was half-emptied of the treated water. At the chemical oxygen demand (COD), total nitrogen (TN), and total phosphorus (TP) loading rates on the total biofilm area of 3.20 g COD, 0.33 g TN, and 0.06 g TP m(-2) d(-1), the removal efficiencies were 97, 85, and 92% for COD, TN, and TP, respectively.  相似文献   

17.
The establishment of nutrient cycles has been widely proposed as a strategy for an efficient management of nutrients such as phosphorus (P). Global reserves of phosphate rocks are limited and are being increasingly depleted. At the same time, P is disposed of via various substance-streams in wastewater treatment. Establishing nutrient cycles may solve these problems and lead to innovative added-value chains with a higher added-value. The objective of this paper is to assess the added-value of P-recovery from sewage sludge via struvite precipitation and its application as fertilizer in Berlin-Brandenburg (Germany). The added-value from struvite precipitation was determined by performing a cost/benefit analysis based on data from standardized questionnaires and interviews with operators of wastewater treatment facilities. Surveys of 146 farmers were used to ascertain what crops were cultivated in the study area and to gauge the willingness of farmers to substitute struvite for conventional mineral P-fertilizer. Benefits from using struvite were found by calculating the fertilizer costs when struvite is substituted for conventional mineral fertilizer. The results indicate that the precipitation of struvite and its use as fertilizer generates added-value gains for wastewater treatment facilities (416,000 €) and for crop producers (35,000 €). In wastewater treatment, struvite precipitation reduces operating costs and yields additional revenues through struvite sales. In crop production, fertilization costs are reduced by substituting struvite for mineral P-, N- and Ca-fertilizers. The distribution of the added-value in the struvite value chain is determined by the marketing strategy of struvite. Farmers may obtain a higher share of added-value if struvite is marketed via direct sale.  相似文献   

18.
Biological sulfate reduction was studied in a laboratory-scale anaerobic sequential batch reactor (14 L) containing mineral coal for biomass attachment. The reactor was fed industrial wastewater with increasingly high sulfate concentrations to establish its application limits. Special attention was paid to the use of butanol in the sulfate reduction that originated from melamine resin production. This product was used as the main organic amendment to support the biological process. The reactor was operated for 65 cycles (48 h each) at sulfate loading rates ranging from 2.2 to 23.8 g SO(4)(2-)/cycle, which corresponds to sulfate concentrations of 0.25, 0.5, 1.0, 2.0 and 3.0 g SO(4)(2-) L(-1). The sulfate removal efficiency reached 99% at concentrations of 0.25, 0.5 and 1.0 g SO(4)(2-) L(-1). At higher sulfate concentrations (2.0 and 3.0 g SO(4)(2-) L(-1)), the sulfate conversion remained in the range of 71-95%. The results demonstrate the potential applicability of butanol as the carbon source for the biological treatment of sulfate in an anaerobic batch reactor.  相似文献   

19.
陈玉谷  白威 《四川环境》1992,11(4):8-13
采用中温(34±2℃)全混合式厌氧反应器处理蒽酸和硫化烧碱草浆造纸黑液。对比厌氧发酵结合物化前或后处理两种方法进行试验,厌氧生物降解COD_(er)去除率分别为61.2~75.3%和34.9~46.2%,COD_(er)总去除率分别为80.0~87.6%和68.4~75.8%。在厌氧发酵稳态运行条件下,对发酵污泥中主要微生物类群和数量进行了研究。  相似文献   

20.
A polyaluminum chloride (PAC) coagulant was prepared from AlCl3 x 6H2O and Na2CO3. The Al13 species in PAC was separated and purified by the SO4(2-)/Ba2+ deposition-replacement method, and characterized by 27Al-NMR and XRD. From 27Al-NMR spectroscopy, it was found that PAC obtained after separation and purification contained more Al13 (PAC-Al13, for short) than original PAC before separation and purification. In XRD spectra, a strong Al13 signal appeared in the range of 2theta from 5 to 25 degrees. Jar tests were performed to test the coagulation efficiency of AlCl3, PAC and PAC-Al13 in treating synthetic or actual water samples. Compared with PAC and AlCl3, PAC-Al13 gives the best results for turbidity, humic acid and color removal, and achieves the highest charge-neutralizing ability. Under the study conditions, PAC-Al13 gave about 90% humic acid removal and almost 100% reactive blue dye removal when its dosages were 4.0 and 15 mg/L as Al, respectively. The Al13 species has a higher positive charge and is the most effective polymeric Al species in water and wastewater treatment.  相似文献   

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