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1.
Abstract

Efforts to develop multipollutant control strategies have demonstrated that adding certain oxidants to different classes of Ca-based sorbents leads to a significant improvement in elemental Hg vapor (Hg0), SO2, and NOx removal from simulated flue gases. In the study presented here, two classes of Ca-based sorbents (hydrated limes and silicate compounds) were investigated. A number of oxidizing additives at different concentrations were used in the Ca-based sorbent production process. The Hg0, SO2, and NOx capture capacities of these oxidant-enriched sorbents were evaluated and compared to those of a commercially available activated carbon in bench-scale, fixed-bed, and fluid-bed systems. Calcium-based sorbents prepared with two oxidants, designated C and M, exhibited Hg0 sorp-tion capacities (~100 μg/g) comparable to that of the activated carbon; they showed far superior SO2 and NOx sorption capacities. Preliminary cost estimates for the process utilizing these novel sorbents indicate potential for substantial lowering of control costs, as compared with other processes currently used or considered for control of Hg0, SO2, and NOx emissions from coal-fired boilers. The implications of these findings toward development of multipollutant control technologies and planned pilot and field evaluations of more promising multipollutant sorbents are summarily discussed.  相似文献   

2.
Abstract

The reaction between three different Ca-based sorbents and SO2 were studied in a medium temperature range (473–773 K). The largest SO2 capture was found with Ca(OH)2 at 773 K, 126.31 mg SO2?g Ca(OH)2 ?1, and the influence of SO2 concentration on the sorbent utilization was observed. Investigations of the internal porous structure of Ca-based sorbents showed that the initial reaction rate was controlled by the surface area, and once the sul-fated products were produced, pore structure dominated. To increase the surface area of Ca-based sorbents available to interact with and retain SO2, one kind of CaO/activated carbon (AC) sorbent/catalyst was prepared to study the effect of AC on the dispersion of Ca-based materials. The results indicated that the Ca-based material dispersed on high-surface-area AC had more capacities for SO2 than unsupported Ca-based sorbents. The initial reaction rates of the reaction between SO2 and Ca-based sorbents and the prepared CaO/AC sorbents/cata-lysts were measured. Results showed that the reaction rate apparently increased with the presence of AC. It was concluded that CaO/AC was the active material in the des-ulfurization reaction. AC acting as the support can play a role to supply O2 to increase the affinity to SO2. Moreover, when AC is acting as a support, the surface oxygen functional group formed on the surface of AC can serve as a new site for SO2 adsorption.  相似文献   

3.

Activated carbon was one of the main adsorptions utilized in elemental mercury (Hg0) removal from coal combustion flue gas. However, the high cost and low physical adsorption efficiency of activated carbon injection (ACI) limited its application. In this study, an ultra-high efficiency (nearly 100%) catalyst sorbent-Sex/Activated carbon (Sex/AC) was synthesized and applied to remove Hg0 in the simulated flue gas, which exhibited 120 times outstanding adsorption performance versus the conventional activated carbon. The Sex/AC reached 17.98 mg/g Hg0 adsorption capacity at 160 °C under the pure nitrogen atmosphere. Moreover, it maintained an excellent mercury adsorption tolerance, reaching the efficiency of Hg0 removal above 85% at the NO and SO2 conditions in a bench-scale fixed-bed reactor. Characterized by the multiple methods, including BET, XRD, XPS, kinetic and thermodynamic analysis, and the DFT calculation, we demonstrated that the ultrahigh mercury removal performance originated from the activated Se species in Sex/AC. Chemical adsorption plays a dominant role in Hg0 removal: Selenium anchored on the surface of AC would capture Hg0 in the flue gas to form an extremely stable substance-HgSe, avoiding subsequent Hg0 released. Additionally, the oxygen-containing functional groups in AC and the higher BET areas promote the conversion of Hg0 to HgO. This work provided a novel and highly efficient carbon-based sorbent -Sex/AC to capture the mercury in coal combustion flue gas.

Selenium-modified porous activated carbon and the interface functional group promotes the synergistic effect of physical adsorption and chemical adsorption to promote the adsorption capacity of Hg0.

  相似文献   

4.
Abstract

Bench-scale testing of elemental mercury (Hg0) sorption on selected activated carbon sorbents was conducted to develop a better understanding of the interaction among the sorbent, flue gas constituents, and Hg0. The results of the fixed-bed testing under simulated lignite combustion flue gas composition for activated carbons showed some initial breakthrough followed by increased mercury (Hg) capture for up to ~4.8 hr. After breakthrough, the Hg in the effluent stream was primarily in an oxidized form (>90%). Aliquots of selected activated carbons were exposed to simulated flue gas containing Hg0 vapor for varying time intervals to explore surface chemistry changes as the initial breakthrough, Hg capture, and oxidation occurred. The samples were analyzed by X-ray photoelectron spectroscopy to determine changes in the abundance and forms of sulfur, chlorine, oxygen, and nitrogen moieties as a result of interactions of flue gas components on the activated carbon surface during the sorption process. The data are best explained by a competition between the bound hydrogen chloride (HCl) and increasing sulfur [S(VI)] for a basic carbon binding site. Because loss of HCl is also coincident with Hg breakthrough or loss of the divalent Hg ion (Hg2+), the competition of Hg2+ with S(VI) on the basic carbon site is also implied. Thus, the role of the acid gases in Hg capture and release can be explained.  相似文献   

5.
Abstract

Selective catalytic reduction (SCR) technology increasingly is being applied for controlling emissions of nitrogen oxides (NOx) from coal-fired boilers. Some recent field and pilot studies suggest that the operation of SCR could affect the chemical form of mercury (Hg) in coal combustion flue gases. The speciation of Hg is an important factor influencing the control and environmental fate of Hg emissions from coal combustion. The vanadium and titanium oxides, used commonly in the vanadia-titania SCR catalyst for catalytic NOx reduction, promote the formation of oxidized mercury (Hg2+).

The work reported in this paper focuses on the impact of SCR on elemental mercury (Hg0) oxidation. Bench-scale experiments were conducted to investigate Hg0 oxidation in the presence of simulated coal combustion flue gases and under SCR reaction conditions. Flue gas mixtures with different concentrations of hydrogen chloride (HCl) and sulfur dioxide (SO2) for simulating the combustion of bituminous coals and subbituminous coals were tested in these experiments. The effects of HCl and SO2 in the flue gases on Hg0 oxidation under SCR reaction conditions were studied. It was observed that HCl is the most critical flue gas component that causes conversion of Hg0 to Hg2+ under SCR reaction conditions. The importance of HCl for Hg0 oxidation found in the present study provides the scientific basis for the apparent coal-type dependence observed for Hg0 oxidation occurring across the SCR reactors in the field.  相似文献   

6.
Abstract

This paper is particularly related to elemental mercury (Hg0) oxidation and divalent mercury (Hg2+) reduction under simulated flue gas conditions in the presence of nitric oxide (NO) and sulfur dioxide (SO2). As a powerful oxidant and chlorinating reagent, Cl2 has the potential for Hg oxidation. However, the detailed mechanism for the interactions, especially among chlorine (Cl)-containing species, SO2, NO, as well as H2O, remains ambiguous. Research described in this paper therefore focused on the impacts of SO2 and NO on Hg0 oxidation and Hg2+ reduction with the intent of unraveling unrecognized interactions among Cl species, SO2, and NO most importantly in the presence of H2O. The experimental results demonstrated that SO2 and NO had pronounced inhibitory effects on Hg0 oxidation at high temperatures when H2O was also present in the gas blend. Such a demonstration was further confirmed by the reduction of Hg2+ back into its elemental form. Data revealed that SO2 and NO were capable of promoting homogeneous reduction of Hg2+ to Hg0 with H2O being present. However, the above inhibition or promotion disappeared under homogeneous conditions when H2O was removed from the gas blend.  相似文献   

7.
Abstract

An entrained-flow system has been designed and constructed to simulate in-flight mercury (Hg) capture by sorbent injection in ducts of coal-fired utility plants. The test conditions of 1.2-sec residence time, 140 °C gas temperature, 6.7 m/sec (22 ft/sec) gas velocity, and 0–0.24 g/m3 (0–15 lbs of sorbent per 1 million actual cubic feet of flue gas [lb/MMacf]) sorbent injection rates were chosen to simulate conditions in the ducts. Four kinds of sorbents were used in this study. Darco Hg-LH served as a benchmark sorbent with which Hg control capability of other sorbents could be compared. Also, Darco-FGD was used as a representative raw activated carbon sorbent. Two different copper chloride-impregnated sorbents were developed in our laboratory and tested in the entrained-flow system to examine the possibility of using these sorbents at coal-fired power plants. The test results showed that one of the copper chloride sorbents has remarkable elemental mercury (Hg0) oxidation capability, and the other sorbent demonstrated a better performance in Hg removal than Darco Hg-LH.  相似文献   

8.
Abstract

Injection of powdered activated carbon (PAC) upstream of particulate removal devices (such as electrostatic precipitator and baghouses) has been used effectively to remove hazardous air pollutants, particularly mercury-containing pollutants, emitted from combustors and incinerators. Compared with commercial PACs (CPACs), an alternative PAC derived from waste tires (WPAC) was prepared for this study. The equilibrium adsorptive capacity of mercury chloride (HgCl2) vapor onto the WPAC was further evaluated with a self-designed bench-scale adsorption column system. The adsorption temperatures investigated in the adsorption column were controlled at 25 and 150 °C. The superficial velocity and residence time of the flow were 0.01 m/sec and 4 sec, respectively. The adsorption column tests were run under nitrogen gas flow. Experimental results showed that WPAC with higher Brunauer–Emmett–Teller (BET) surface area could adsorb more HgCl2 at room temperature. The equilibrium adsorptive capacity of HgCl2 for WPAC measured in this study was 1.49 × 10?1 mg HgCl2/g PAC at 25 °C with an initial HgCl2 concentration of 25 μg/m3. With the increase of adsorption temperature ≤150 °C, the equilibrium adsorptive capacity of HgCl2 for WPAC was decreased to 1.×34 10?1 mg HgCl2/g PA≤C. Furthermore,WPAC with higher sulfur contents could adsorb even more HgCl2 because of the reactions between sulfur and Hg2+ at 150 °C. It was demonstrated that the mechanisms for adsorbing HgCl2 onto WPAC were physical adsorption and chemisorption at 25 and 150 °C, respectively. Experimental results also indicated that the apparent overall driving force model appeared to have the good correlation with correlation coefficients (r) >0.998 for HgCl2 adsorption at 25 and 150 °C. Moreover, the equilibrium adsorptive capacity of HgCl2 for virgin WPAC was similar to that for CPAC at 25 °C, whereas it was slightly higher for sulfurized WPAC than for CPAC at 150 °C.  相似文献   

9.
Fe2O3 and CeO2 modified activated coke (AC) synthesized by the equivalent-volume impregnation were employed to remove elemental mercury (Hg0) from simulated flue gas at a low temperature. Effects of the mass ratio of Fe2O3 and CeO2, reaction temperature, and individual flue gas components including O2, NO, SO2, and H2O (g) on Hg0 removal efficiency of impregnated AC were investigated. The samples were characterized by Brunauer–Emmett–Teller (BET), X-ray diffraction (XRD), scanning electron microscopy (SEM), and X-ray photoelectron spectroscopy (XPS). Results showed that with optimal mass percentage of 3 % Fe2O3 and 3 % CeO2 on Fe3Ce3/AC, the Hg0 removal efficiency could reach an average of 88.29 % at 110 °C. Besides, it was observed that O2 and NO exhibited a promotional effect on Hg0 removal, H2O (g) exerted a suppressive effect, and SO2 showed an insignificant inhibition without O2 to some extent. The analysis of XPS indicated that the main species of mercury on used Fe3Ce3/AC was HgO, which implied that adsorption and catalytic oxidation were both included in Hg0 removal. Furthermore, the lattice oxygen, chemisorbed oxygen, and/or weakly bonded oxygen species made a contribution to Hg0 oxidation.  相似文献   

10.
湿式烟气脱硫系统同时脱汞研究   总被引:3,自引:0,他引:3  
研究表明,湿法烟气脱硫装置(WFGD)可去除烟气中绝大部分Hg2+,但对单质汞的吸收效果不明显,因此研究提高湿法烟气脱硫系统中单质汞的氧化率的方法对控制汞的排放具有重要意义。综述了WFGD及在此系统中各种添加剂的脱汞性能,认为在添加剂中,气态的臭氧、液态的次氯酸和氯化钠稀溶液、 黄磷乳浊液、氢硫化钠溶液及EDTA的汞去除效果较好,且不会被SO2大量消耗,可在WFGD系统实现同时脱硫脱汞;而气态的氯气,液态的K2S2O8溶液虽然也有较好的汞去除效果,但因易被SO2或亚硫酸盐溶液消耗,当在WFGD系统中用其氧化单质汞时,需要对脱硫塔进行分层或其他改造,使烟气中的SO2被吸收后再控制汞,提高经济性。  相似文献   

11.
Observations of reactive gaseous mercury (RGM) in marine air show a consistent diurnal cycle with minimum at night, rapid increase at sunrise, maximum at midday, and rapid decline in afternoon. We use a box model for the marine boundary layer (MBL) to interpret these observations in terms of RGM sources and sinks. The morning rise and midday maximum are consistent with oxidation of elemental mercury (Hg0) by Br atoms, requiring <2 ppt BrO in most conditions. Oxidation of Hg0 by Br accounts for 35–60% of the RGM source in our model MBL, with most of the remainder contributed by oxidation of Hg0 by ozone (5–20%) and entrainment of RGM-rich air from the free troposphere (25–40%). Oxidation of Hg0 by Cl is minor (3–7%), and oxidation by OH cannot reproduce the observed RGM diurnal cycle, suggesting that it is unimportant. Fitting the RGM observations could be achieved in the model without oxidation of Hg0 by ozone (leaving Br as the only significant oxidant) by increasing the entrainment flux from the free troposphere. The large relative diurnal amplitude of RGM concentrations implies rapid loss with a lifetime of only a few hours. We show that this can be quantitatively explained by rapid, mass-transfer-limited uptake of RGM into sea-salt aerosols as HgCl3? and HgCl42?. Our results suggest that 80–95% of HgII in the MBL should be present in sea-salt aerosol rather than gas-phase, and that deposition of sea-salt aerosols is the major pathway delivering HgII to the ocean.  相似文献   

12.
A previously proposed technology incorporating TiO2 into common household fluorescent lighting was further tested for its Hg0 removal capability in a simulated flue-gas system. The flue gas is simulated by the addition of O2, SO2, HCl, NO, H2O, and Hg0, which are frequently found in combustion facilities such as waste incinerators and coal-fired power plants. In the O2 + N2 + Hg0 environment, a Hg0 removal efficiency (ηHg) greater than 95% was achieved. Despite the tendency for ηHg to decrease with increasing SO2 and HCl, no significant drop was observed at the tested level (SO2: 5–300 ppmv, HCl: 30–120 ppmv). In terms of NO and moisture, a significant negative effect on ηHg was observed for both factors. NO eliminated the OH radical on the TiO2 surface, whereas water vapor caused either the occupation of active sites available to Hg0 or the reduction of Hg0 by free electron. However, the negative effect of NO was minimized (ηHg > 90%) by increasing the residence time in the photochemical reactor. The moisture effect can be avoided by installing a water trap before the flue gas enters the Hg0 removal system.

Implications: This paper reports a novel technology for a removal of gas-phase elemental mercury (Hg0) from a simulated flue gas using TiO2-coated glass beads under a low-cost, easily maintainable household fluorescent light instead of ultraviolet (UV) light. In this study, the effects of individual chemical species (O2, SO2, HCl, NO, and water vapor) on the performance of the proposed technology for Hg0 removal are investigated. The result suggests that the proposed technology can be highly effective, even in real combustion environments such as waste incinerators and coal-fired power plants.  相似文献   

13.
Abstract

Most of the synthetic gypsum generated from wet flue gas desulfurization (FGD) scrubbers is currently being used for wallboard production. Because oxidized mercury is readily captured by the wet FGD scrubber, and coal-fired power plants equipped with wet scrubbers desire to benefit from the partial mercury control that these systems provide, some mercury is likely to be bound in with the FGD gypsum and wallboard. In this study, the feasibility of identifying mercury species in the FGD gypsum and wallboard samples was investigated using a large sample size thermal desorption method. Potential candidates of pure mercury standards including mercuric chloride (HgCl2), mercurous chloride (Hg2Cl2), mercury oxide (HgO), mercury sulfide (HgS), and mercuric sulfate (HgSO4) were analyzed to compare their results with those obtained from FGD gypsum and dry wallboard samples. Although any of the thermal evolutionary curves obtained from these pure mercury standards did not exactly match with those of the FGD gypsum and wallboard samples, it was identified that Hg2Cl2 and HgCl2 could be candidates. An additional chlorine analysis from the gypsum and wallboard samples indicated that the chlorine concentrations were approximately 2 orders of magnitude higher than the mercury concentrations, suggesting possible chlorine association with mercury.  相似文献   

14.
Efforts to develop multipollutant control strategies have demonstrated that adding certain oxidants to different classes of Ca-based sorbents leads to a significant improvement in elemental Hg vapor (Hg0), SO2, and NOx removal from simulated flue gases. In the study presented here, two classes of Ca-based sorbents (hydrated limes and silicate compounds) were investigated. A number of oxidizing additives at different concentrations were used in the Ca-based sorbent production process. The Hg0, SO2, and NOx capture capacities of these oxidant-enriched sorbents were evaluated and compared to those of a commercially available activated carbon in bench-scale, fixed-bed, and fluid-bed systems. Calcium-based sorbents prepared with two oxidants, designated C and M, exhibited Hg0 sorption capacities (approximately 100 microg/g) comparable to that of the activated carbon; they showed far superior SO2 and NOx sorption capacities. Preliminary cost estimates for the process utilizing these novel sorbents indicate potential for substantial lowering of control costs, as compared with other processes currently used or considered for control of Hg0, SO2, and NOx emissions from coal-fired boilers. The implications of these findings toward development of multipollutant control technologies and planned pilot and field evaluations of more promising multipollutant sorbents are summarily discussed.  相似文献   

15.
Sodium hypochlorite (NaClO) has been widely used as a chemical additive for enhancing nitrogen oxide (NOx; NO + NO2), sulfur dioxide (SO2), and mercury (Hg0) removals in a wet scrubber. However, they are each uniquely dependent on NaClO(aq) pH, hence making the simultaneous control difficult. In order to overcome this weakness, we sprayed low liquid-to-gas (L/G) ratio (0.1 L/Nm3) of NaClO(aq) to vaporize quickly at 165 °C. Results have shown that the maximized NOx, SO2, and Hg0 removals can be achieved at the pH range between 4.0 and 6.0. When NOx and Hg0 coexist with SO2, in addition, their removals are significantly enhanced by reactions with solid and gaseous by-products such as NaClO(s), NaClO2(s), OClO, ClO, and Cl species, originated from the reaction between SO2 and NaClO(aq). We have also demonstrated the feasibility of this approach in the real flue gases of a combustion plant and observed 50%, 80%, and 60% of NOx, SO2, and Hg0 removals, respectively. These findings led us to conclude that the spray of NaClO(aq) at a relatively high temperature at which the sprayed solution can vaporize quickly makes the simultaneous control of NOx, SO2, and Hg0 possible.

Implications: The simple spray of NaClO(aq) at temperatures above 165 °C can cause the simultaneous removal of gaseous NOx, SO2, and Hg0 by its quick vaporization. Their maximized removals are achieved at the pH range between 4.0 and 6.0. NOx and Hg0 removals are also enhanced by gaseous and solid intermediate products generated from the reaction of SO2 with NaClO(aq). The feasibility of this approach has been demonstrated in the real flue gases of a combustion plant.  相似文献   


16.
EPA’s efforts to develop low cost, retrofitable flue gas cleaning technology include the development of highly reactive sorbents. Recent work addressing lime enhancement and testing at the bench-scale followed by evaluation of the more promising sorbents in a pilot plant are discussed here.

The conversion of Ca(OH)2 with SO2 increased several-fold compared with Ca(OH)2 alone when Ca(OH)2 was slurrled with fly ash first and later exposed to SO2 in a laboratory packed bed reactor. Ca(OH)2 enhancement increased with the increased fly ash amount. Dlatomaceous earths were very effective reactivity promoters of lime-based sorbents. Differential scanning calorimetry of the promoted sorbents revealed the formation of a new phase (calcium silicate hydrates) after hydration, which may be the basis for the observed Improved SO2 capture.

Fly ash/lime and diatomaceous earth/lime sorbents were tested in a 100 m3/h pilot facility incorporating a gas humidifier, a sorbent duct injection system, and a baghouse. The inlet SO2 concentration range was 1000-2500 ppm. With once-through dry sorbent injection into the humidified flue gas [approach to saturation 10–20°C (18–36°F) in the baghouse], the total SO2 removal ranged from 50 to 90 percent for a stoichiometric ratio of 1 to 2. Recycling the collected solids resulted in a total lime utilization exceeding 80–90 percent. Increased lime utilization was also investigated by the use of additives.  相似文献   

17.
Si L  Ariya PA 《Chemosphere》2011,84(8):1079-1084
Mercury is a global environmental contaminant with severe toxicity impact. The chemical processes resulting in the transformation of oxidized mercury species (Hg2+) to elemental mercury (Hg0), greatly affects the fate and transport of mercury in the natural environment. We hereby provide the first study on the photochemistry of Hg2+ with selected alkanethiols (R-SH) as model compounds to represent thiols and thiol-type binding sites on humic substances in natural waters because of the common sulfhydryl functional group (-SH). Kinetic studies were performed using cold vapor atomic fluorescence spectroscopy (CVAFS), the formation of Hg2+-thiol complexes (Hg(SR)2) were confirmed by UV-visible spectrometry and Atmospheric Pressure Chemical Ionization-Mass Spectrometry (APCI-MS), and the reaction products were analyzed using Electron Impact-Mass Spectrometry (EI-MS) and Solid Phase Microextraction coupled with Gas Chromatography-Mass Spectrometry (SPME/GC-MS). Our results indicated that the photoreduction of Hg2+ by selected alkanethiols may be mediated by Hg2+-thiol complexes to produce Hg0. Under our experimental conditions, the apparent first order rate constants obtained for 1-propanethiol, 1-butanethiol, and 1-pentanethiol were (2.0 ± 0.2) × 10−7 s−1, (1.4 ± 0.1) × 10−7 s−1, (8.3 ± 0.5) × 10−8 s−1, respectively. The effects of ionic strength, dissolved oxygen or chloride ion on reaction rates were found to be minimal under our experimental conditions. The identified products of the reaction between oxidized mercury species with selected alkanethiols (C3-C5) were Hg0 and disulfides (RS-SR). The potential environmental implications are herein discussed.  相似文献   

18.
Concentrations of different species of mercury in arctic air and precipitation have been measured at Ny-Ålesund (Svalbard) and Pallas (Finland) during 1996–1997. Typical concentrations for vapour phase mercury measured at the two stations were in the range of 0.7–2 ng m−3 whereas particulate mercury concentrations were below 5 pg m−3. Total mercury in precipitation was in the range 3–30 ng l−1. In order to evaluate the transport and deposition of mercury to the arctic from European anthropogenic sources, the Eulerian transport model HMET has been modified and extended to also include mercury species. A scheme for chemical conversion of elemental mercury to other species of mercury and deposition characteristics of different mercury species have been included in the model. European emission inventories for three different forms of Hg (Hg0, HgCl2 and Hgp) have been implemented in the numerical grid system for the HMET model.  相似文献   

19.
This study examines gaseous chlorinated species generated from the reaction of sulfur dioxide (SO2) with sodium chlorite powder (NaClO2(s)) to obtain insight into the propensity of this process to enhance NO and Hg0 oxidation. A packed bed reactor containing NaClO2(s) was used and the reaction temperature was set to 130 °C. Initially, we determined that the presence of SO2 enhances the oxidation of NO and Hg0 by reaction with NaClO2(s). We then introduced NO2 into the gas mixture as a radical scavenger and determined that the chlorinated species generated by the reaction of SO2 with NaClO2(s) are OClO, Cl, ClO, and Cl2. Based on these results, we suggest that such gaseous chlorinated ones are responsible for the enhancement of NO and Hg0 oxidation.  相似文献   

20.
Incident radiation has been reported to facilitate mercury release from soils. In this study the influence of light on mercury emissions from substrates amended with pure synthetic mercury species, and from naturally and anthropogenically mercury-enriched substrates were investigated using laboratory experiments and in situ flux measurements. Light-enhanced emissions were found to occur from substrates amended with HgS, and from elemental mercury (Hg0) and HgCl2 amended iron oxide and organic containing substrates. The magnitude of light-enhanced emissions for natural substrates ranged from 1.5 to 116 times that occurring in the dark at the same substrate temperature. Substrates containing corderoite, metacinnabar and “matrix bound mercury” (that bound to organic or inorganic phases) exhibited a higher degree of light-enhanced emissions relative to that containing predominantly cinnabar. Calculated activation energies for both laboratory and field data indicate that photo-reduction is a process associated with the light-enhanced emissions. Activation energies, derived using in situ mercury fluxes and soil temperatures, indicated that photo-reduction was a dominant process facilitating release of Hg from substrates with sunrise. Activation energies, calculated using daytime data, were less than those calculated for sunrise. This is hypothesized to be due to a pool of Hg0 being developed with photo-reduction at first light that is released as soil temperatures and convective heat transfer increase during the day. This study demonstrated that light energy is the more dominant process controlling mercury emissions from naturally enriched substrates than soil temperature.  相似文献   

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