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1.
A laboratory scale two-stage sequencing batch reactor (TSSBR) was used to study the effectiveness of pH as a real-time control parameter in swine wastewater treatment. A Ringlace media was inserted into the A/O (Anoxic/Oxic) reactor for bacteria immobilization. The TSSBR was subjected to three levels of organic loading. The pH and ORP (Oxidation Reduction Potential) patterns obtained were consistent with distinct features, enabling the real-time control strategy to effectively set a flexible aeration time pending on influent concentration, hence resulting in flexible cycle time and HRT (Hydraulic Retention Time) for the system. The real-time process ensured a removal efficiency of over 99% and 95%, respectively, for ammonia and TOC (Total Organic Carbon). For NO3(-)-N and PO4(-3), the run with influent TOC = 4,000 mg/L yielded the most efficient removal of 61% and 95%, respectively. Test results suggest that pH can be a viable tool for on-line real-time control of a biological treatment process.  相似文献   

2.
Abstract

A laboratory scale two‐stage sequencing batch reactor (TSSBR) was used to study the effectiveness of pH as a real‐time control parameter in swine wastewater treatment. A Ringlace media was inserted into the A/O (Anoxic/Oxic) reactor for bacteria immobilization. The TSSBR was subjected to three levels of organic loading. The pH and ORP (Oxidation Reduction Potential) patterns obtained were consistent with distinct features, enabling the real‐time control strategy to effectively set a flexible aeration time pending on influent concentration, hence resulting in flexible cycle time and HRT (Hydraulic Retention Time) for the system. The real‐time process ensured a removal efficiency of over 99% and 95%, respectively, for ammonia and TOC (Total Organic Carbon). For NO3 ‐N and PO4 ‐3, the run with influent TOC = 4,000 mg/L yielded the most efficient removal of 61% and 95%, respectively. Test results suggest that pH can be a viable tool for on‐line real‐time control of a biological treatment process.  相似文献   

3.
This study compared the swine wastewater treatment of two identical lab-scale two-stage sequencing batch reactors (TSSBR) under similar conditions except that one was operated on a fixed-time mode and the other on a real-time mode. While both TSSBR systems performed very well, the real-time TSSBR performed far better then the fixed-time TSSBR, in every aspect of carbon, nitrogen, and phosphorous removal. The removals of COD, TOC, were at 97% and for BOD5 even at 99.7%. In terms of NH4-N and TKN removals, the real-time TSSBR achieved removal of over 98%. For phosphorus removals (Ortho-P and total P) the results from the real-time TSSBR was quite remarkable at 97.7%.  相似文献   

4.
Abstract

This study compared the swine wastewater treatment of two identical lab-scale two-stage sequencing batch reactors (TSSBR) under similar conditions except that one was operated on a fixed-time mode and the other on a real-time mode. While both TSSBR systems performed very well, the real-time TSSBR performed far better then the fixed-time TSSBR, in every aspect of carbon, nitrogen, and phosphorous removal. The removals of COD, TOC, were at 97% and for BOD5 even at 99.7%. In terms of NH4-N and TKN removals, the real-time TSSBR achieved removal of over 98%. For phosphorus removals (Ortho-P and total P) the results from the real-time TSSBR was quite remarkable at 97.7%.  相似文献   

5.
张衍  郑炜  刘锐  李伟  李荧  陈吕军 《环境工程学报》2012,6(12):4355-4360
对化学合成橡胶碱洗废水进行了有机组分和可生化性分析,废水主要含有氯甲烷、六甲苯、异丁醇、甲醇等污染物质,生化降解实验中废水TOC可在6 d内从60.9 mg/L下降至0.0 mg/L,可生化降解性好,适于生化处理。选择混凝-生物接触氧化组合工艺对废水进行处理,采用优化条件(pH=8、PAC=40 mg/L、PAM=8 mg/L)进行混凝,碱洗废水COD去除率为9.95%~72.94%(平均31.51%);混凝后的碱洗废水与冲洗废水1∶5混合进行接触氧化处理,在HRT为36 h的情况下,COD去除率为65.6%~72.6%(平均70.4%),出水COD为134~331 mg/L,满足企业废水排放市政管网的要求;同时,实验发现COD去除率与COD容积负荷存在指数函数变化关系。  相似文献   

6.
The main objective of this study was to investigate the feasibility of coagulation as a post-treatment method of anaerobically treated primary municipal wastewater. Both mesophilic and ambient (20 degrees C) temperature conditions were investigated in a laboratory-scale upflow anaerobic sludge bed (UASB) reactor. In addition, optimization of the coagulant, both in terms of type and dose, was performed. Finally, phosphorus removal by means of aluminum and iron coagulation and phosphorus and ammonia nitrogen removal by means of struvite precipitation were studied. Anaerobic treatment of primary effluent at low hydraulic retention times (less than 15 hours) resulted in mean chemical oxygen demand (COD) removals ranging from 50 to 70%, while, based on the filtered treated effluent, the mean removals increased to 65 to 80%. Alum coagulation of the UASB effluent gave suspended solids removals ranging from approximately 35 to 65%. Turbidity removal reached up to 80%. Remaining COD values after coagulation and settling were below 100 mg/L, while remaining total organic carbon (TOC) levels were below 50 mg/L. Filterable COD levels were generally below 60 mg/L, while filterable TOC levels were below 40 mg/L. All coagulants tested, including prepolymerized aluminum and iron coagulants, demonstrated similar efficiency compared with alum for the removal of suspended solids, COD, and TOC. Regarding struvite precipitation, optimal conditions for phosphorus and nitrogen removal were pH 10 and molar ratio of magnesium: ammonia-nitrogen: phosphate-phosphorus close to the stoichiometric ratio (1:1:1). During struvite precipitation, removal of suspended solids reached 40%, while turbidity removal reached values up to 80%. The removal of COD was approximately 30 to 35%; yet, when removal of organic matter was based on the treated filterable COD, the removal increased to approximately 65%. In addition, nitrogen was removed by approximately 70%, while phosphorus removal ranged between approximately 30 and 45% on the basis of the initial phosphorus concentration. Finally, size fractionation of the organic matter (COD) showed that the various treatment methods were capable of removing different fractions of the organic matter.  相似文献   

7.
利用Ce-Fe/Al2O3为催化剂的非均相光Fenton体系降解阳离子红GTL模拟废水,考察了H2O2浓度、催化剂用量、初始pH值及不同工艺过程对降解效果的影响,通过紫外-可见漫反射光谱、红外光谱、XPS手段研究铁在反应中的价态变化。结果表明,在11 W低压汞灯照射下,非均相光Fenton体系能够有效地降解结构稳定的阳离子红GTL,在pH 6,反应温度20℃,时间90 min,Ce-Fe/Al2O3 2 g/L,H2O2浓度340 mg/L,含50 mg/L阳离子红GTL模拟废水TOC去除率为92.40%;光Fenton反应中Fe(Ⅲ)转化为Fe(Ⅱ)。  相似文献   

8.
采用双氧水在常温常压下对实验室模拟的高浓度含硫废水进行处理,考察了双氧水的浓度、初始pH和反应时间对硫化物去除效果的影响,以及含硫废水去除过程中氧化还原电位(ORP)的控制对氧化产物的影响,分析了固相产物的晶体和表面结构。结果表明,在双氧水浓度为0.147 mol/L、初始pH为6、反应时间为9 min的条件下,废水中硫化物浓度由1985.46 mg/L降至38.37 mg/L,硫化物去除率达到98.07%,去除效果最佳。在初始ORP值不同的条件下,体系中主要的氧化产物为单质硫和硫酸根;当加入的氧化剂不足时,单质硫和硫酸根随ORP值降低而增加,当加入氧化剂过量时,单质硫和硫酸根随ORP值增加而增加;当体系中ORP值控制在60~178 mV时,单质硫的产量都能达到较为理想的值。X射线衍射(XRD)分析表明,体系中固相产物为环状斜方硫(α-硫)。扫描电子显微镜(SEM)分析表明,单质硫颗粒为表面不光滑的球状颗粒,粒径呈微米级,越小越易聚集在一起。  相似文献   

9.
两级SBR与传统SBR工艺的对比研究   总被引:2,自引:0,他引:2  
用两级SBR工艺(TSSBR)处理COD与氮浓度较高的工业废水,SBR1去除有机物,SBR2主要进行硝化反硝化。TSSBR与传统SBR工艺相比,COD降解速率和硝化反应速率明显提高,COD去除率由84%提高到93%,2种工艺的反硝化速率没有明显差别。在原水COD浓度较高的情况下,TSSBR可有效克服高COD浓度对硝化反应的抑制,硝化反应速率是传统SBR的2倍。对于COD和氮浓度较高的工业废水,TSSBR明显优于传统SBR,是一种理想的处理工艺。  相似文献   

10.
A laboratory-scale study was conducted using a completely mixed reactor with a constant influent-total-organic carbon (TOC) of 3750 mg/L to evaluate the effect of increasing influent-sulfate levels on anaerobic-treatment performance. The sulfate levels were increased stepwise from 333 to 666, 1000, 1333 and 1666 mg S/L. The results showed that an elevation of influent sulfate actually increased the TOC removal efficiency as long as the produced sulfide level did not induce toxicity. At 1333 mg S/L influent sulfate, the produced dissolved sulfide was 613 mg S/L (free sulfide = 228 mg S/L), which started to impose toxicity to the methane-producing bacteria (MPB). It was also found that the percent electron flow to the sulfate-reducing pathway increased with the increasing influent sulfate, but the direction toward the methanogenesis was correspondingly reduced. Nevertheless, under the experimental conditions tested, the majority of the influent organics was still degraded through the methanogenic pathway. Through this study, an oxidation-reduction-potential (ORP)-based oxygenation process was developed for online oxidation of sulfide in recirculating biogas. With controlled oxygen injection to raise the reactor's ORP by 25 mV, the residual sulfide in the reactor was almost totally eliminated. In case of over oxygenation, any excess oxygen was quickly consumed by the facultative organisms in the reactor, thereby imposing no toxicity to the MPB.  相似文献   

11.
采用活性炭吸附和两级Fenton氧化组合工艺对高盐度对氨基苯酚生产废水进行了处理实验研究。结果表明,pH值对活性炭去除有机物的影响较小。当活性炭投加量为4 g/L时,TOC去除率61%。分级加药可以有效提高Fenton氧化对有机物的去除效率。在温度为25℃、pH为3、30% H2O2投加量为3%(V/V)、Fe2+/H2O2摩尔比为0.05时,两级Fenton氧化处理后,出水TOC降至150 mg/L以下。此外,Fenton氧化后形成氢氧化铁污泥颗粒粒径为4.5 μm,经过聚丙烯酰胺(PAM)絮凝之后,污泥的粒径明显增加,过滤特性改善。PAM絮凝效果依赖于溶液的pH值,当pH超过10后会失去作用,故在使用过程中需要严格控制溶液的pH值。  相似文献   

12.
The ORP and pH profiles and the stability of Simultaneous Nitrification and Denitrification (SND) for low carbon municipal wastewater treatment were investigated under the different aeration modes in Sequencing Batch Reactor (SBR). The results showed that the 92% removal efficiency for TN, the smallest average level of ORP and both of the variation of ORP and pH values are achieved in Intermittent Aeration (IA) with 0.5 aeration fraction and high air-on frequency. These results suggested that IA with small aeration fraction and high air-on frequency favourable for the stable SND. The average level of ORP fluctuation range and the stability of ORP and pH values are all beneficial for the stable and complete degree of SND.  相似文献   

13.
采用两级SBR工艺(TSSBR)处理COD与氮浓度较高的工业废水,SBR1去除有机物,SBR2主要进行硝化反硝化。TSSBR与传统SBR工艺相比,COD降解速率和硝化反应速率明显提高,COD去除率由84%提高到93%,2种工艺的反硝化速率没有明显差别。在原水COD浓度较高的情况下,TSSBR可有效克服高COD浓度对硝化反应的抑制,硝化反应速率是传统SBR的2倍。对于COD和氮浓度较高的工业废水,TSSBR明显优于传统SBR,是一种理想的处理工艺。  相似文献   

14.
采用SBBR在溶解氧1.0 mg/L条件下考察了不同温度对实际炼油催化剂废水脱氮系统效能的影响.结果表明,SBBR容积负荷及同步硝化反硝化(SND)三氮去除率与进水氨氮浓度正相关.不同进水浓度下,反应器SND三氮去除率最高可达40%左右.33、30及28℃条件下,反应器亚硝积累率均可稳定保持在90%以上.不同温度下短程硝化反硝化pH值及ORP变化趋势基本一致,结合在线监控pH值及ORP变化规律调控反应时间,最大限度保证短程硝化的稳定性.  相似文献   

15.
市政污泥水热炭化废水组成成分特征   总被引:1,自引:0,他引:1  
污泥水热炭化处理被认为是极具潜力的污泥安全处置与资源化利用的技术措施之一。为了解废水中碳、氮、磷、钾和重金属含量随水热炭化反应温度和反应时间的变化规律,对市政污泥190℃和260℃水热炭化不同时间(1、6、12、18和24 h)后的废水组成成分进行了研究。结果表明,水热炭化处理后,废水颜色由黑色变成浅黄色;pH由6.40提高到9.14;TOC、COD和BOD5最高分别增加了13 175 mg/L、55 998 O2mg/L和31 723 O2mg/L;氮和钾含量显著提高,但磷含量降低;Cd、Cr含量由未检测到分别增加到0.060 mg/L和2.326 mg/L,As、Pb含量均由0.032 mg/L分别增加到1.408 mg/L和0.590 mg/L,但Cu、Mn及Zn含量降低。比起反应时间,反应温度对废水组成成分的影响更大。  相似文献   

16.
Three municipal wastewater treatment plants (WWTPs) in southeastern Pennsylvania were sampled to determine the presence and concentrations of 12 natural and synthetic estrogen hormones in the wastewater influent and effluent. The target estrogens were 17alpha-estradiol, estrone, estriol, equilin, 17alpha-dihydroequilin, 17beta-estradiol, 17alpha-ethinyl estradiol, gestodene, norgestrel, levonorgestrel, medrogestone, and trimegestone. One WWTP uses a biofilm reactor (packed-bed trickling filter),and the other two use suspended-growth media (continuously stirred activated sludge reactor and sequential batch reactor). Estrone was detected in all the three plants; estriol and estradiol were detected at two WWTPs; and 17 alpha-dihydroequilin and 17 alpha-ethinyl estradiol were detected at one WWTP. The concentration of estrogens in the influent and effluent of the three treatment plants ranged from 1.2 to 259 ng/L and 0.5 to 49 ng/L, respectively. The percentage removal of estrogens from the aqueous phase ranged from 41 to 99%, except in the case of 17alpha-dihydroequilin; the removal of 17alpha-dihydroequilin was negligible. The suspended-growth media systems showed higher removal efficiencies for estrogens than the biofilm system. The analytical method uses a Varian C-18 solid-phase extraction (Varian Inc., Palo Alto, California), followed by a derivatization with bis(trimethylsilyl)trifluoroacetamide. The detection limits for the estrogen compounds ranged from 0.1 to 10 ng/L using a sample size of 1 L. The method recoveries ranged from 71 to 120%, and the relative standard deviation ranged from 6 to 14% for all the hormones.  相似文献   

17.
Real-time control of aeration tank operation is key to high-efficiency pollutant removal and energy savings. One of the aims of this study was to examine the potential for using redox potential (oxidation-reduction potential [ORP]) to indicate wastewater quality online in aeration tanks treating medium (chemical oxygen demand [COD] of 70 to 150 mg/L) and low (COD of 15 to 30 mg/L) pollutant-concentration wastewaters. The field-scale data provide a good relationship between ORP values and nutrient removal along the length of the aeration tanks. The ORP values increased dramatically as organic matter was removed along the aeration tanks, indicating the improvement of the bulk liquor redox status. Dissolved oxygen higher than 1.0 mg/L was necessary for good biodegradation and improvement of the liquid redox status. Nitrification occurred at higher ORP values (380 to 420 mV) than was the case for organic substrate oxidation (250 to 300 mV). The microprofiles obtained from microelectrode measurements substantiate the heterogeneity of the microbial processes inside activated sludge flocs. Because of microbial oxygen utilization, the aerobic region in the activated sludge floc was limited to the top layer (0.1 to 0.2 mm) of the activated sludge aggregate present in medium-strength wastewater, with an anoxic zone dominating inside the flocs. When dissolved oxygen in the bulk water was higher than 4.0 mg/L, the anoxic zone inside the floc disappeared. At low wastewater pollutant concentrations, the ORP and dissolved oxygen inside the activated sludge aggregates were higher than those from medium-strength wastewater. The prospect of using ORP as an online control approach for aeration tank operation and the potential reasons for activated sludge floc size varying with pollutant strengths are also discussed.  相似文献   

18.
为了实现脉冲SBR深度脱氮的实时控制,以某污水处理厂市政污水为处理对象,考察了脉冲SBR在深度脱氮过程中pH及ORP的变化规律.试验结果表明,pH及ORP的变化规律与脉冲SBR有机物去除、硝化与反硝化过程存在较好的相关关系.可以根据pH和ORP变化曲线上的特征点对脉冲SBR进行实时控制.并考察了污水C/N(COD/NH4 -N)对pH及ORP的变化规律的影响.在硝化过程中,C/N对pH及ORP曲线变化点的出现没有影响;在反硝化过程中,应结合pH值"硝酸盐峰"和ORP"硝酸盐膝"来判断低C/N污水反硝化的终点.在该试验中,出水TN低于2 mg/L,TN去除率可达到96%以上.  相似文献   

19.
臭氧/ 生物活性炭深度处理循环养殖废水   总被引:5,自引:0,他引:5  
随着工厂化循环水养殖的不断发展,高浓度循环养殖废水对环境污染日益严重.为实现环境友好和资源节约,采用臭氧/生物活性炭对循环养殖废水进行深度处理中试研究.实验结果表明,臭氧化臭氧最佳投加量为4 mg/L,显著增强水体的可生化性,使TOC(总有机碳)/UV254(在波长为254 nm处的单位比色皿光程下的紫外吸光度)提高80%.臭氧/生物活性炭对循环养殖废水中的有机物和氨氮具有良好的去除效果.臭氧/生物活性炭对TOC、高锰酸盐指数和UV254的最终去除率比生物活性炭分别高11.9%、13.4%和6.5%.臭氧/生物活性炭和生物活性炭对氨氮的最终去除率分别为96.0%、90.7%.  相似文献   

20.
A method for estimation of the maximum substrate utilization rate (q(max)) using batch reactors with denitrification biofilm was introduced and compared with the traditional method of using batch reactors with suspended growth for q(max) estimation. The values of q(max) obtained from the suspended-growth reactors (0.69 to 0.71 g N/g volatile suspended solids [VSS] x d) and from the attached-biomass reactors (0.74 to 0.85 g N/g VSS x d) are similar and within the range of the values reported in the literature (0.23 to 2.88 g N/g VSS x d). Therefore, the intrinsic kinetic parameter, q(max), can be obtained using attached-growth batch reactors, if the effectiveness factor, eta, is approximately equal to 1 and the bulk concentration of the rate-limiting substrate, C, is much higher than the half-velocity constant, K(S). The attached-growth batch reactor method is unique, because the biomass used in the batch tests is the same as that present in the parent reactor under investigation.  相似文献   

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