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1.
不同形式(常压,增压)的硫化床锅炉,应用的脱硫吸收剂种类不同,根据硫化床炉内脱硫的机理,推导炉内脱硫设计计算公式,对硫化床锅炉本体热力计算具有一定的价值。  相似文献   

2.
介绍了循环流化床锅炉配置的CEMS,此时的CEMS不仅是大气污染物监测的一种测量系统,并且可为脱硫系统的脱硫剂投放提供参考数据,以此监控脱硫效率。  相似文献   

3.
介绍了循环流化床锅炉燃用煤泥的燃烧调整方法,阐述了燃用煤泥技术对电厂降低成本,提高经济效益及社会效益的积极意义。  相似文献   

4.
为预测油页岩粒度、床温、钙硫比、床中灰分含量等参数对流化床二氧化硫排放量的影响,本文开发了耦合油页岩燃烧放硫、石灰石固硫和灰粒固硫的综合模型,并将该模型的预测值与实验结果进行了比较,发现两者吻合良好。本文的工作是研究工业化连续式油页岩流化床燃烧脱硫的基础,对茂名建设5万千瓦油页岩流化床燃烧热电站有重要的参考价值,并对于研究煤的燃烧利用有借鉴意义。  相似文献   

5.
循环流化床锅炉脱硫工艺对烟尘性质的影响   总被引:1,自引:0,他引:1  
介绍循环流化床锅炉脱硫工艺特点,及其对烟尘质量浓度,粉径分布,形态,粘性比电阻等物理,化学特性的影响。  相似文献   

6.
循环流化床锅炉脱硫技术与烟气脱硫技术经济分析   总被引:1,自引:0,他引:1  
为改善大气质量,现有火电厂利用其有限场地寻求一种初投资省,占地少,脱硫率高、技术成熟可靠,运行成本低的脱硫装置势在必行。本文以广西合山电厂100MW机组为例对脱硫技改工程进行技术经济分析,以获得最佳脱硫方式,为决策提供依据。  相似文献   

7.
增压流化床燃烧联合循环是一种新型燃烧热力发电技术,它具有高效低污染的突出优点。本文分析了增压流化床燃烧联合循环中NOX,SOX,CO,CO2的形成过程,介绍了控制增压流化床燃烧联合循环的NOX,SOX,CO,CO2和粉尘排放的最新研究成果。  相似文献   

8.
循环流化床锅炉的烟气和烟尘性质与常规煤粉炉相比有较大差异。针对循环流化床烟尘特性.分析其对电除尘器除尘效率可能造成的影响,提出电除尘器的设计要求,并对应用工程实例进行了分析。  相似文献   

9.
10.
循环流化床燃烧技术的环境效益初探   总被引:2,自引:0,他引:2  
通过计算,总结了河南省采用循环流化床锅炉所取得的环境效益,为循环流化床锅炉的应用提供参考。  相似文献   

11.
以水为吸收液,采用旋转填充床分离微生物厌氧发酵沼气中的CO_2,考察了工艺条件对CO_2吸收效果的影响。实验结果表明:进液量越大、气液比越小、进口CO_2体积分数越小、操作压力越大、进液温度越低则CO_2的吸收效果越好,而床转速以适中为宜;在进液量60 L/h、气液比3.3、床转速1 000 r/min、进口CO_2体积分数40%、操作压力1.2 MPa、进液温度5℃的条件下,CO_2吸收率为57.4%,提纯后气体的CO_2体积分数为17%。  相似文献   

12.
利用扫描电镜、激光粒度分析、X-衍射分析等测试手段,对循环流化床粉煤灰的理化性质和微观结构进行分析。比较了5种激发剂对循环流化床粉煤灰的激发效果,结果表明Na2SiO3·9H2O的激发效果最好。  相似文献   

13.
The use of plastic bags and film packaging is very frequent in manifold sectors and film waste is usually present in different sources of municipal and industrial wastes. A significant part of it is not suitable for mechanical recycling but could be safely transformed into a valuable gas by means of thermal valorization. In this research, the gasification of film wastes has been experimentally investigated through experiments in a fluidized bed reactor of two reference polymers, polyethylene and polypropylene, and actual post-consumer film waste. After a complete experimental characterization of the three materials, several gasification experiments have been performed to analyze the influence of the fuel and of equivalence ratio on gas production and composition, on tar generation and on efficiency. The experiments prove that film waste and analogue polymer derived wastes can be successfully gasified in a fluidized bed reactor, yielding a gas with a higher heating value in a range from 3.6 to 5.6 MJ/m3 and cold gas efficiencies up to 60%.  相似文献   

14.
The incinerator at the T.Z. Osborne Plant in Greensboro, North Carolina burns sludge from its own waste water treatment plant and sludge pumped from the nearby North Buffalo plant. The two plants have a combined capacity of 36 million gallons per day of wastewater. Because of the age of and increasing high maintenance on the existing multiple hearth incinerator, and the need to increase treatment capacity, the Osborne plant concluded a study in 1992 evaluating its options for future municipal sewage sludge disposal. Options which were evaluated during the study included; (i) rehabilitation of the existing eight-year old multiple hearth unit; (ii) addition of a new multiple hearth; (iii) addition of a new fluid bed system; (iv) drying, composting, or land application. The chosen option, based on both economic and environmental considerations, was a new fluid bed system with a capacity of 2.55 tons per hour, approximately double that of the existing multiple hearth. Design of the new fluid bed system began in December 1994 and equipment delivery for the incineration system was begun in April 1995. Initial operation occurred in August 1996. Primary and secondary sludge, dewatered to 28% dry solids by centrifuge, is delivered by piston pumps to the twenty-foot freeboard ID incinerator. A shell and tube heat exchanger recuperates heat from the exhaust gas and preheats the combustion air to 1250°F, resulting in minimal auxiliary fuel use. The air pollution control device is a high-energy Tandem Nozzle® scrubber. Greensboro was the initial installation of this scrubber design on a fluid bed incinerator and its characteristics and performance are discussed. Ash is dewatered in an ash thickener/belt press system prior to disposal to landfill. The system includes a state of the art Programmable Logic Controller (PLC) system for computer control of the operation. The unit was commissioned in August 1996 and has been in continuous operation since that time except for a one week inspection and maintenance shutdown in February 1999. The plant operates 24 h/day, 7 days per week. The initial performance test showed the system to readily meet federal and state air emission standards. Particulate released was 0.002 grains per dry standard cubic foot, carbon monoxide was 22.5 parts per million volumetric (ppmv) and opacity was 0.4%. These results show a significant emission reduction with the fluid bed when compared to the multiple hearth. Annual tests conducted since then and continuous emission monitoring have shown the unit to be in consistent compliance. Since the fluid bed system became operational, the old multiple hearth system has been maintained on standby as a backup, but its use has not been required. Operational experience is discussed, the most interesting of which is the relatively trouble-free operation. The minor problems which occurred and their solutions are detailed. Also included is a comparison of operation and maintenance experience of the fluid bed and the multiple hearth. Current sludge disposal actual cost data are also provided including the average cost per ton of dry solids treated. The almost three years of operational experience to date has shown that the decision to install a new fluid bed system was the correct one on both an environmental and economic basis. It has provided benefits to all interested parties — the wastewater treatment plant, the regulators, the taxpayers, and the surrounding community.  相似文献   

15.
对选择性非催化还原(SNCR)烟气脱硝技术与选择性催化还原(SCR)烟气脱硝技术在流化床锅炉上应用的适应性进行了对比分析。分析结果显示,相对于SCR技术,SNCR技术更适于流化床锅炉,指出了SNCR技术在流化床锅炉上应用存在的问题,N2O难以去除。  相似文献   

16.
介绍了流化床富氧焚烧含油污泥技术的流程和优势,计算了富氧焚烧含油污泥系统主要设备的电耗和技术经济指标。流化床富氧焚烧含油污泥技术可实现烟气及其他污染物零排放,产生的蒸汽可直接供应油田生产和生活使用,产生的液态CO2可直接用于油井驱油,烟气中的SO2和NOx可转化为硫酸和硝酸。采用日处理200 t含油污泥的流化床锅炉年处理含油污泥量约73 kt,每年减少排污费7 300万元;锅炉年产蒸汽量约177 kt,每年节约蒸汽费用1 380.6万元,合计每年节约成本8 680.6万元。回收得到质量分数为40%的稀硫酸5.56 t/d,质量分数为37%的硝酸0.708 t/d,年回收CO2约99 kt。  相似文献   

17.
小龙潭发电厂烟气循环流化床脱硫工程评述   总被引:4,自引:0,他引:4  
张凤兰  程岩 《电力环境保护》2003,19(1):22-24,50
阐述了小龙潭发电厂100MW机组烟气脱硫工程的工艺原理、系统流程、主要设备等,并结合系统调试过程中发现的问题,对该工艺的运行调试进行了评述。  相似文献   

18.
常佳伟  樊金梦  王伟  赵磊  邵磊 《化工环保》2012,40(2):131-136
以旋转填充床(RPB)为反应器,采用臭氧氧化工艺处理实际兰炭废水一级生化池出水。考察了臭氧浓度、RPB转速、气液比、初始废水pH、废水温度和RPB处理级数对废水处理效果和臭氧利用率的影响。实验得到的适宜工艺条件为:保持进气流量90 L/h不变,不调节废水pH和温度,控制臭氧质量浓度50 mg/L、气液比5∶1、RPB转速1 500 r/min,进行二级处理。在上述工艺条件下,处理COD为340.0 mg/L、BOD5/COD为0.18、pH为7.77、温度为24.7 ℃的废水,处理后出水COD去除率为19.7%,BOD5/COD为0.34,可生化性大幅提高,可满足后续生化处理要求。  相似文献   

19.
介绍了彭城电厂回流式循环流化床烟气脱硫的主要设计参数及工艺流程,并对运行中需注意的一些问题进行了分析与探讨。  相似文献   

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