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21.
介绍了管帏冲击式除尘器的结构及其捕尘机理。介绍了对该除尘器进行除尘和防淋雨性能测试的实验方法和装置。分析了实验数据,得出了相应的结论。  相似文献   
22.
降尘监测可以较客观地反映与评价城市区域扬尘污染水平。及时掌握降尘污染状况,对区域扬尘污染治理措施成效和评价城市区域环境空气质量具有实际意义。降尘监测具有采样设备简单、操作简便易行、成本相对较低等特点。但是监测周期长、环节多等都会影响降尘监测的准确性。本文通过对吴泾工业区扬尘污染治理中降尘数据分析发现,降尘监测中存在降尘数据波动大、受周边环境影响大、人为损坏多等诸多因素的影响,就这些影响因素进行分析探讨,并提出了若干建议和解决方法。  相似文献   
23.
以电-袋复合式除尘器为仿真研究对象,在Windows界面下利用Visual Basic6.0编程语言开发出燃煤电厂电-袋复合式除尘器优化控制的仿真运行软件。该软件通过建立数学模型,进行仿真实验,模拟工况变化、优化运行参数等对电-袋复合除尘系统进行整体的优化控制,并综合分析电-袋复合除尘器运行过程中的能耗以及运行费用,对运行电压、电流、运行阻力、喷吹周期等参数进行了优化。该仿真软件达到了电一袋除尘系统的节能降耗的目的,同时也降低了电~袋复合除尘器的运行成本。  相似文献   
24.
Ash deposition impact on the energy performance of photovoltaic generators   总被引:1,自引:0,他引:1  
A little known side effect of the atmospheric air pollution is the degradation of photovoltaic (PV) cells’ performance due to the deposition of solid particles varying in composition, size and origin. In this context, an experimental-based investigation is conducted in order to compare the energy performance of two identical pairs of PV-panels; the first being clean and the second being artificially polluted with ash, i.e. a by-product of incomplete hydrocarbons’ combustion mainly originating from thermal power stations and vehicular exhausts. A series of systematic measurements of current intensity, voltage output and solar radiation are executed simultaneously for the clean and the polluted PV-panel, so that the effect of several mass depositions on the PVs’ power output, energy yield and conversion efficiency may be determined. According to the results, a considerable deterioration of the PV-panels’ performance is obtained, i.e. almost 30% energy reduction per hour or 1.5% efficiency decrease (in absolute terms) for ash accumulation on the panels’ surface reaching up to 0.4 mg/cm2.  相似文献   
25.
林炜  许明海 《环境工程》2011,29(1):121-122,41
由于半干法脱硫工艺对布袋除尘器的特殊要求,使得其配套的布袋除尘器构造不同于以往常规的布袋除尘器.从布袋除尘器的过滤风速、滤料选择、沉降室设置、布风均匀性、灰斗特性、旁路系统的要求做详细的说明.  相似文献   
26.
Fire and explosion accidents are frequently caused by combustible dust, which has led to increased interest in this area of research. Although scholars have performed some research in this field, they often ignored interesting phenomena in their experiments. In this paper, we established a 2D numerical method to thoroughly investigate the particle motion and distribution before ignition. The optimal time for the corn starch dust cloud to ignite was determined in a semi-closed tube, and the characteristics of the flame propagation and temperature field were investigated after ignition inside and outside the tube. From the simulation, certain unexpected phenomena that occurred in the experiment were explained, and some suggestions were proposed for future experiments. The results from the simulation showed that 60–70 ms was the best time for the dust cloud to ignite. The local high-temperature flame clusters were caused by the agglomeration of high-temperature particles, and there were no flames near the wall of the tube due to particles gathering and attaching to the wall. Vortices formed around the nozzle, where the particle concentration was low and the flame spread slowly. During the explosion venting, particles flew out of the tube before the flame. The venting flame exhibited a “mushroom cloud” shape due to interactions with the vortex, and the flame maintained this shape as it was driven upward by the vortex.  相似文献   
27.
为了使电炉烟气治理过程中污染源的排放达到国家排放标准,提出一种TSLCDM长袋低压脉冲除尘器(简称TSLCDM除尘器)。通过对该除尘器结构、除尘原理以及不同工况下除尘效率和过滤阻力的分析,得到该除尘器的除尘效率>99.9%,压力损失<1200 Pa,最终排出的烟气含尘质量浓度约5.54 mg/m3,满足了国家的超低排放要求,以泉州某公司电炉项目除尘系统为研究对象,证明了该新型脉冲布袋除尘器在电炉烟气治理除尘系统的应用效果,具有很好的经济和环境效益。  相似文献   
28.
The effect of pyrolysis and oxidation characteristics on the explosion sensitivity and severity parameters, including the minimum ignition energy MIE, minimum ignition temperature MIT, minimum explosion concentration MEC, maximum explosion pressure Pmax, maximum rate of pressure rise (dP/dt)max and deflagration index Kst, of lauric acid and stearic acid dust clouds was experimentally investigated. A synchronous thermal analyser was used to test the particle thermal characteristics. The functional test apparatuses including the 1.2 L Hartmann-tube apparatus, modified Godbert-Greenwald furnace, and 20 L explosion apparatus were used to test the explosion parameters. The results indicated that the rapid and slow weight loss processes of lauric acid dust followed a one-dimensional diffusion model (D1 model) and a 1.5 order chemical reaction model (F1.5 model), respectively. In addition, the rapid and slow weight loss processes of stearic acid followed a 1.5 order chemical reaction model (F1.5 model) and a three-dimensional diffusion model (D3 model), respectively, and the corresponding average apparent activation energy E and pre-exponential factor A were larger than those of lauric acid. The stearic acid dust explosion had higher values of MIE and MIT, which were mainly dependent on the higher pyrolysis and oxidation temperatures and the larger apparent activation energy E determining the slower rate of chemical bond breakage during pyrolysis and oxidation. In contrast, the lauric acid dust explosion had a higher MEC related to a smaller pre-exponential factor A with a lower amount of released reaction heat and a lower heat release rate during pyrolysis and oxidation. Additionally, due to the competition regime of the higher oxidation reaction heat release and greater consumption of oxygen during explosion, the explosion pressure Pm of the stearic acid dust was larger in low concentration ranges and decayed to an even smaller pressure than with lauric acid when the concentration exceeded 500 g/m3. The rate of explosion pressure rise (dP/dt)m of the stearic acid dust was always larger in the experimental concentration range. The stearic acid dust explosion possessed a higher Pmax, (dP/dt)max and Kst mainly because of a larger pre-exponential factor A related to more active sites participating in the pyrolysis and oxidation reaction. Consequently, the active chemical reaction occurred more violently, and the temperature and overpressure rose faster, indicating a higher explosion hazard class for stearic acid dust.  相似文献   
29.
There is a noticeable discrepancy in the ability to control reduced explosion overpressure between flat bursting panels and curved bursting panels with the same static activation overpressure. Flat bursting plates were observed to leak at approximately 80% of the static activation overpressure lower than curved bursting plates. A new experimental technique is proposed in our paper. Three different vent areas of flat and curved bursting panels were tested, there was significant difference in structural stiffness between flat bursting panels and curved bursting panels, which is the reason the discrepancy in the ability to control reduced explosion overpressure. The structural stiffness of the flat bursting panels is poorer than that of the other, and a greater deformation of the flat bursting panels occurs under the same load. The membrane stress caused by the explosion overpressure therefore produces a larger value in the flat bursting panels which causes it to open prematurely. Moreover, the smaller the vent area that is, the more significant discrepancy in controlling the reduced explosion overpressure between both bursting panels is. This experimental and theoretical result in our paper provides some useful experience for the method of explosion venting.  相似文献   
30.
According to standard procedures, flammability and explosion parameters for dusts and dust mixtures are evaluated in 20 L and/or 1 m3 vessels, with equivalent results provided a correct ignition delay time (60 ms in the 20 L vessel; 600 ms in the 1 m3 vessel). In this work, CFD simulations of flow field and dust concentration distribution in the 1 m3 spherical vessel are performed, and the results compared to the data previously obtained for the 20 L. It has been found that in the 1 m3 vessel, the spatial distribution of the turbulent kinetic energy is lower and much more uniform. Concerning the dust distribution, as in the case of the 20 L, dust is mainly concentrated at the outer zones of the vortices generated inside the vessel. Furthermore, an incomplete feeding is attained, with most of the dust trapped in the perforated annular nozzle. Starting from the maps of dust concentration and turbulent kinetic energy, the deflagration index KSt is calculated in both vessels. In the conditions of the present work, the KSt is found to be 2.4 times higher in the 20 L than in the 1 m3 vessel.  相似文献   
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