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Environmental Science and Pollution Research - Systematic reviews are a more complete, repeatable, and less biased form of literature reviews leading to evidence-based conclusions. A systematic...  相似文献   
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Data reconciliation and mass balance analysis were conducted for the first time to improve the data obtained from a petrochemical wastewater treatment plant (WWTP), and the results were applied to evaluate the performance of the plant. Daily average values for 209 days from the inlet and outlet of the plant obtained from WWTP documentation center along with the results of four sampling runs in this work were used for data reconciliation and performance evaluation of the plant. Results showed that standard deviation and relative errors in the balanced data of each measurement decreased, especially for the process wastewater from 24.5 to 8.6 % for flow and 24.5 to 1.5 % for chemical oxygen demand (COD). The errors of measured data were −137 m3/day (−4.41 %) and 281 kg/day (7.92 %) for flow and COD, respectively. According to the balanced data, the removal rates of COD and 5-day biological oxygen demand (BOD5) through the aeration unit were equal to 37 and 46 %, respectively. In addition, the COD and BOD5 concentrations were reduced by about 61.9 % (2137 kg/day) and 78.1 % (1976 kg/day), respectively, prior to the biological process. At the same time, the removal rates of benzene, toluene, and styrene were 56, 38, and 69 %, respectively. The results revealed that about 40 % of influent benzene (75.5 kg/day) is emitted to the ambient air at the overhead of the equalization basin. It can be concluded that the volatilization of organic compounds is the basic mechanism for the removal of volatile organic compounds (VOCs) and it corresponds to the main part of total COD removal from the WWTP.

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Biological treatment of waste gas styrene vapor was investigated in a three-stage bench-scale biofilter. Yard waste compost mixed with shredded hard plastics in a 25:75 v/v ratio of plastics:compost was inoculated with thickened municipal activated sludge. Microbial acclimation to styrene was achieved by exposing the system to an inlet concentration (C(In)) of 0.25 gm(-3) styrene and an empty bed retention time (EBRT) of 360 s for 30 days. Under steady-state conditions, maximum elimination capacity (EC) obtained was 45 gm(-3)h(-1) at a loading rate (L) of 60 gm(-3)h(-1) (C(In) of 2 gm(-3) and EBRT of 120 s). Reduction of retention time adversely impacted the performance resulting in the maximum EC of 39 and 27 gm(-3)h(-1) for EBRT of 60 and 30 s, respectively. Evaluation of the concentration profile along the bed height indicated dominance of first-order kinetics at C(In) < or = 0.45 gm(-3) and zero-order for higher concentrations.  相似文献   
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