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超重力旋转填料床中络合铁脱硫工艺处理海上油田含硫伴生天然气
引用本文:胡徐彦.超重力旋转填料床中络合铁脱硫工艺处理海上油田含硫伴生天然气[J].化工环保,2014,35(3):254-256.
作者姓名:胡徐彦
作者单位:中海石油(中国)有限公司湛江分公司,广东湛江524057
摘    要:采用超重力旋转填料床中络合铁脱硫工艺处理海上油田伴生天然气。运行结果表明:海上油田超重力旋转填料床络合铁脱硫系统投资1 500 万元,设备总占用面积不足48 m2,天然气处理量2×105 m3/d,回收硫磺400 kg/d;进口伴生天然气中硫化氢的质量浓度为2 000~2 500 mg/L,经脱硫处理后硫化氢的质量浓度低于3 mg/L,达到GB 17820—2012《天然气》中硫化氢含量的要求。该工艺解决了海上平台空间紧张、结构承重有限等问题,装置运行稳定,避免了设备腐蚀,运行成本低,运行效果显著,具有良好的经济效益和社会效益。

关 键 词:海上油田  含硫伴生天然气  脱硫工艺  超重力  络合铁  
收稿时间:2013-11-29

Treatment of Offshore Oilfield Associated Gas by Complex iron Desulfurization in High Gravity Rotating Packed Bed
Hu Xuyan.Treatment of Offshore Oilfield Associated Gas by Complex iron Desulfurization in High Gravity Rotating Packed Bed[J].Environmental Protection of Chemical Industry,2014,35(3):254-256.
Authors:Hu Xuyan
Institution:Zhanjiang Branch,CNOOC,Zhanjiang Guangdong 524057,China
Abstract:The offshore oilfield associated gas was treated by complex iron desulfurization process in a high gravity rotating packed bed. The project investment of the desulfurization system is 15 million yuan;The total equipment occupation area is less than 48 m2,the treatment capacity of natural gas is 2×105 m3/d and the sulfur recovery is 400 kg/d;the hydrogen sulfide mass concentration of the inlet gas is 2 000-2 500 mg/L,and that of the treated gas is lower than 3 mg/L,which can meet the requirements of GB 17820-2012 for hydrogen sulfide mass concentration of natural gas. The results show that the process is characterized by small area need,light weight,stable operation,good anticorrosion,low operation cost,good treatment effect,and good economic and social benefits.
Keywords:offshore oilfield  sulfur-containing associated gas  desulfurization process  high gravity  complex iron  
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