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好氧/厌氧潜流湿地结构工艺优化
引用本文:李锋民,单时,李媛媛,李扬,王震宇.好氧/厌氧潜流湿地结构工艺优化[J].环境科学,2012,33(2):436-441.
作者姓名:李锋民  单时  李媛媛  李扬  王震宇
作者单位:中国海洋大学环境科学与工程学院,海洋环境与生态教育部重点实验室,青岛 266100;中国海洋大学环境科学与工程学院,海洋环境与生态教育部重点实验室,青岛 266100;中国海洋大学环境科学与工程学院,海洋环境与生态教育部重点实验室,青岛 266100;中国海洋大学环境科学与工程学院,海洋环境与生态教育部重点实验室,青岛 266100;中国海洋大学环境科学与工程学院,海洋环境与生态教育部重点实验室,青岛 266100
基金项目:国家自然科学基金项目(40906053); 国家水体污染控制与治理科技重大专项(2009ZX07010-009,2009ZX07010-008); 青岛市科技发展计划(10-3-3-21-nsh)
摘    要:前期研究表明在人工潜流湿地(SFCWs)中设置好氧段和厌氧段可显著提高SFCWs对COD、NH4+-N的去除率.然而曝气产生的富氧环境不利于NO3--N和NO2--N的去除,一定程度上抑制了反硝化反应的进行.反硝化程度较低是实验中仍需进一步解决的问题.本研究在前期研究的基础上,对好氧/厌氧多级串联潜流人工湿地结构及工艺进行了改进优化,采用多点进水的措施来强化反硝化过程,并设计相应的区段去除该部分污染物.结果表明,水力负荷约为0.06m3.(m2.d)-1时,进一步优化结构和比例的好氧-缓冲-厌氧-缺氧-好氧曝气多点进水湿地对COD、NH4+-N和TN的去除率可达到91.6%、100%和87.7%.在补充进水之后的区段,COD/N迅速升高到10以上,做到了补充碳源的同时最大限度地利用湿地去除污染物.改良后的湿地达到了净化工艺优化的目的,为提高人工湿地总氮去除效率提供了理论依据及应用基础.

关 键 词:好氧/厌氧串联  补充进水  碳氮比  总氮去除率  优化
修稿时间:2011/5/21 0:00:00

Optimization of Aerobic/Anaerobic Subsurface Flow Constructed Wetlands
LI Feng-min,SHAN Shi,LI Yuan-yuan,LI Yang and WANG Zheng-yu.Optimization of Aerobic/Anaerobic Subsurface Flow Constructed Wetlands[J].Chinese Journal of Environmental Science,2012,33(2):436-441.
Authors:LI Feng-min  SHAN Shi  LI Yuan-yuan  LI Yang and WANG Zheng-yu
Institution:Key Laboratory of Marine Environment and Ecology, Ministry of Education, College of Environmental Science and Engineering, Ocean University of China, Qingdao 266100, China;Key Laboratory of Marine Environment and Ecology, Ministry of Education, College of Environmental Science and Engineering, Ocean University of China, Qingdao 266100, China;Key Laboratory of Marine Environment and Ecology, Ministry of Education, College of Environmental Science and Engineering, Ocean University of China, Qingdao 266100, China;Key Laboratory of Marine Environment and Ecology, Ministry of Education, College of Environmental Science and Engineering, Ocean University of China, Qingdao 266100, China;Key Laboratory of Marine Environment and Ecology, Ministry of Education, College of Environmental Science and Engineering, Ocean University of China, Qingdao 266100, China
Abstract:Previous studies showed that setting aerobic and anaerobic paragraph segments in the subsurface constructed wetlands (SFCWs) can improve the COD, NH4+-N, and TN removal rate, whereas the oxygen enrichment environment which produced by the artificial aeration could restrain the NO3--N and NO2--N removal process, and to a certain extent, inhibit the denitrification in SFCWs Therefore, in this research the structure and technology of SFCW with aerobic and anaerobic paragraph segments were optimized, by using the multi-point water inflow and setting the corresponding section for the extra pollutant removal. Results showed that with the hydraulic load of 0.06 m3·(m2·d)-1, the COD, NH4+-N and TN removal efficiencies in the optimized SFCW achieved 91.6%, 100% and 87.7% respectively. COD/N increased to 10 speedily after the inflow supplement. The multi-point water inflow could add carbon sources, and simultaneously maximum utilization of wetland to remove pollutants. The optimized SFCW could achieve the purposes of purification process optimization, and provide theoretical basis and application foundation for improving the total nitrogen removal efficiency.
Keywords:aerobic/anaerobic  water supplementary  C/N ratio  TN removal efficiency  optimization
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