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某600MW机组AGC控制异常原因分析及处理
引用本文:鲍向东. 某600MW机组AGC控制异常原因分析及处理[J]. 防灾减灾工程学报, 2015, 0(5): 63-65
作者姓名:鲍向东
作者单位:宁夏电投西夏热电有限公司, 宁夏 银川 750021
摘    要:针对某 600 MW 机组自动发电控制(Automatic Generator Control,AGC)运行异常,导致给煤量、给水流量和主汽压力大幅度波动,影响锅炉的安全稳定运行的问题,从磨煤机进出口差压、热风门开度、一次风压值及一次风压调节等方面进行了分析,提出处理措施。分析结果表明:机组 AGC 控制异常的主要原因是一次风量偏小、磨煤机调节能力差所导致的风煤比偏离了设计值,引发锅炉燃烧不稳定。

关 键 词:自动发电控制; 一次风; 风煤比; 磨煤机

Cause analysis and treatment on AGC abnormality for 600 MW unit
BAO Xiangdong. Cause analysis and treatment on AGC abnormality for 600 MW unit[J]. Journal of Disaster Prevention and Mitigation Engineering, 2015, 0(5): 63-65
Authors:BAO Xiangdong
Affiliation:Ningxia Power Investment Co. Xixia Thermal Power Ltd.,Yinchuan Ningxia 750021 ,China
Abstract:Aiming at the problem of the Automatic Generator Control (AGC)running abnormalityfor 600 MW unit,leads to the operating parameters wide fluctuations such as the coal feed rate, the water feed rate and the main steam pressure,influences the safe and steady operation of theboiler,analyzes the inlet and outlet pressure differential of the pulverizer,the hot air port openingdegree,the primary air pressure value and the primary air pressure regulation,etc.,puts forwardtreatment measures. The analysis result shows that the main cause AGC abnormality of the unit isthat small of primary air volume and poor of pulverizer adjustment ability leads coal-air ratio todeviate the design value,and results in the boiler combustion unsteadiness.
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